Resistance
Welder Quick Change Tooling
Kenneth
did this project while he was an employee at an after market and OEM auto parts
manufacturer in Oklahoma City.
It is included to show some of the variety of projects that he has
worked on during his career. At the
manufacturer's chassis products plant, they make a variety of aftermarket and OEM
chassis parts for automobile and light trucks.
Kenneth
worked as a Manufacturing Engineer in the light chassis area.
The light chassis area was divided into three work cells, one of which
was the welder cell, which produced welded ball joints.
The welder cell was a very efficient work area with the exception
changing over from part to part on the welder.
The actual welder was an Atomic brand resistance welder that used a set
of very heavy copper blocks for tooling. These
blocks weighed approximately 25 to 40 pounds apiece.
During each change over both the upper and lower blocks would have to be
changed. Before a good part could
be produced the blocks had to be aligned. Because
each set of blocks were of differing heights, the knee of the welder had to also
be adjusted. The process of
changing the blocks and adjusting the knee usually took an average of 45
minutes.
SCOPE: Kenneth's
assignment was to
develop new tooling that would achieve the following goals:
a.) Reduce the set-up time
of the welder tooling to under 5 minutes
b.) Incorporate existing
alignment pins on the tooling that had ensured product quality
RESULTS: Kenneth accumulated the appropriate dimensional data from every part that was welded in the cell. After doing this and studying both the machine process and existing tooling, he decided to use one set of blocks for every part. The only thing that would have to be changed would be the plates that mounted on the face of each block. These plates were bolted on using socket head cap screws. He decided that instead of using screws pins could be used to keep the plates in place. The existing plates had two alignment pins that helped align each half of the ball joint case. He added two addition pins. This ensured even better quality and increased the life of the replaceable plastic pins. Occasionally the plates would have to be faced and de-burred because of wear. Kenneth added replaceable electrodes that could be easily removed and replaced with new ones. This eliminated the need to send the plates to tool and die for rework. The result of this project was a change over time of 2 or 3 minutes, increased tooling life and better quality ball joints. Below are pictures of the welding cell and weld tooling.
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